On August 16 I took my reactor apart. I don’t have locking rings on my drums; to take my reactor apart I have to cut the top of the barrel off with a cutting disc on my angle grinder, and then to close it back up I have to weld it shut.
Photos 1 through 4 show what I pulled out of the reactor when I tore it down.
Photo 3 in particular shows the warping that my burn tube has experienced. Not good. Not good at all. This is mileage limiting heat and warping.
Still, warping is not cracking, and since I have no alternative, I will just have to keep looking for some suitable burn tube material, and in the meantime keep using what I got.
Now for the modifications: I did a soapy test to check for leaks. I found none, but I reinforced the welds where the nozzles enter the burn tube, lowered the grate to increase the distance from the nozzles to the grate from 7" to 12" (Photo 5 shows this), made an insert to further reduce the restriction from 9" to 6.5", added three layers of sheet metal insulation around my burn tube, and shoved everything back into my 55 gallon drum. This was difficult, and I decided that it would be the last time I would gut my reactor: either I would make this iteration work on the truck, or I would use different inserts to make it work with a small generator after building a working WK reactor.
The results: This time I decided to flare directly off the reactor with no cooling or filtering whatsoever, and then add parts as I got them working. Photo 6 shows the flare that I got straight out of the reactor. Again, I now believe that the fire was higher than the nozzles, because the longer I had things going, the better the flare became. At first it would barely light at all, but as I kept at it, the flare would light when the blower was off, then go out when I turned on the blower. Eventually I could turn the blower on and crack the blower valve just a bit and the flare would stay lit for a couple minutes. I decided to add the cyclone filter.
Kaboom! My first explosion. What happened was my cyclone filter was detached and full of air until I connected it to my reactor. I knew I had to wait a few minutes for the oxygen to blow out of it, but I guess that it never did, because when I lit the flare off the cyclone filter, the flame went down the tube, into the filter drum, and exploded. Luckily my safety caps worked, and one PVC cap was blown up into the air, but that’s all. I shut off the blower, replaced the safety cap, turned the blower back on, and relit the flare. Not a big deal.
I got similar results with the cyclone filter on: flare would stay lit for a couple minutes with the fan on low and the fan valve cracked just a little bit. Any more fan would blow the flare out. I am thinking that I need cleaner, cooler gas to have a stable flare that doesn’t put itself out, so I heartily add the cooling pipes. When I turned the fan back on and tried to light the flare, I got similar results. It would stay lit for about two minutes with the valve cracked just a little. With the fan on low and the valve wide open, I could light the flare with the torch and get three foot flames, but it would go out immediately if I removed the torch. This time the flare was near the ground, so I could set the torch on the ground and the flare would keep burning because of the torch. I wanted to let that run until I ran out of wood, but the zinc compression fitting I had connecting the reactor to the cyclone overheated, melted and finally cracked, which blew woodgas into the air. I decided now was a good time to shut things down and find a better way to join the reactor to the cyclone filter.
Next I would need to make steel flanges to connect my reactor to the cyclone, install a heat exchanger to the system, add to the size of my cooling rack, and install a hay filter of some kind.